The process of converting Locomotive 493 from coal-fired to oil-burning continues. Excellent progress is being made with a great deal of work beginning to come together. Highlights include finishing up portions of the valve motion, rebuilding the rear tender end beam, laying out of the shoe and wedge, finishing UT numbers on the boiler, doing flush patchwork on the firebox, machining driver boxes, and finishing up the spring rigging and reinstallation of various other parts. Cab steelwork is now complete as is the front tender end beam.
Moving forward, the actual assembly of some components such as wheels and running boards may be reinstalled on the locomotive as early as January 2019.
Below are recent highlights of the conversion work:
Installation of Spring Rigging:
In the photo below, roundhouse crew member Will White is working on installing spring rigging.

Completion of Valve Motion Work:
All the parts are off of the engine. Roundhouse crew members have reground the links, made new link blocks, changed out the bushings and the pins, and reset the lever distances. In the photo below, Steve Carr is shown machining valve rings and Joe Dailey is machining valve motion parts.

And below is a photo of the partially rebuilt valve motion.

Completion of Machining of the Driver Boxes:
Below is a photo of 7 of the 8 driver boxes after machining.

And below is a photo of roundhouse crew member, John Walden machining grease grooves in driver box #8.

Completion of UT testing on the boiler:
The UT (ultrasonic testing) is nondestructive testing that measures the thickness of the boiler across many different points. Testing of this kind is done every 15 years. Once completed, these measurements are used to calculate the overall integrity of the boiler. In the photo below you can see the actual measurements of steel thickness at different points written directly on the boiler.

Welding Flush Patch on Firebox:
In the photo below, roundhouse crewmember Anthony Maze welds a flush patch in the firebox.


Last Ride of the Season: October 26th
Due to significant recent weather events, The Durango & Silverton Narrow Gauge Railroad had a slide at milepost 486.0 just north of Needleton which resulted in the tracks being covered with rock and debris, making train passage to Silverton impossible. Due to this, we have had an interruption of service to Silverton and both Silverton trains have been rerouted to Cascade Canyon for tomorrow, July 3rd. resume service to Silverton on July 4th and will be communicating with guests if there is any change. Our maintenance of way crews are actively working to clear the slide and to restore the tracks.
We look forward to restoring full Silverton service on July3 3rd.
We think so, but we’re also a little biased. We’re incredibly thankful to be nominated as one of the “Top 10 Scenic Train Ride in North America” by USA Today! From today until May 13th, you can vote for your all-time favorite scenic train. Do you think we deserve this honorable merit? Then click the link below and vote for the Durango Train! Throughout the duration of the voting period, fans may cast a single vote each day leading up to its conclusion.

We are now operating daily and our train schedule has in fact expanded as we’ve moved deeper into the summer season.
We experienced a brief pause in railroad operations recently while we worked through communications with the Forest Service on our operating status while observing agreed upon fire precautions. Concurrently, we were able to rebook passengers to adjacent days when train excursions were operating.
All trains scheduled for Thursday, June 16 and beyond are operating as scheduled at this time.
Please know that if we experience any interruptions in service due to future fire precaution levels, we will reach out to all of our guests in a most timely manner to offer information and alternatives.
Thank you”
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